Eastern Air Lines Flight 401 | |
Image Upright: | 1.2 |
Occurrence Type: | Accident |
Type: | CFIT due to pilot error and loss of situational awareness |
Site: | Florida Everglades near Miami International Airport Miami-Dade County, Florida, U.S. |
Occupants: | 176 |
Passengers: | 163 |
Crew: | 13 |
Injuries: | 75 |
Fatalities: | 101 (97 initially) |
Survivors: | 75 (79 initially) |
Aircraft Type: | Lockheed L-1011-385-1 TriStar |
Operator: | Eastern Air Lines |
Iata: | EA401 |
Icao: | EAL401 |
Callsign: | EASTERN 401 |
Tail Number: | N310EA |
Origin: | John F. Kennedy Int'l Airport |
Destination: | Miami International Airport |
Eastern Air Lines Flight 401 was a scheduled flight from New York JFK to Miami. Shortly before midnight on December 29, 1972, the Lockheed L-1011-1 TriStar crashed into the Florida Everglades,[1] [2] [3] causing 101 total fatalities. All three cockpit crew members, two of the 10 flight attendants, and 96 of the 163 passengers were killed; 75 people survived.
The crash occurred while the entire flight crew were preoccupied with a burnt-out landing gear indicator light. The captain bumped the control yoke on the aircraft, causing it to turn off the autopilot. Due to the focus on the landing gear and the minimal changes in the cockpit, the pilots did not notice. Because of this, the aircraft gradually lost altitude and crashed. This was the first hull loss and fatal crash of a Lockheed L-1011 TriStar.
Eastern Air Lines Flight 401 was a regularly scheduled flight from John F. Kennedy International Airport in Queens, New York, to Miami International Airport in Miami, Florida. On the day of the crash, Flight 401 was operated using a Lockheed L-1011-1 TriStar (registration N310EA), which had been delivered to the airline on August 18, 1972.[4] The aircraft was fleet number 310, and the 10th TriStar delivered to the carrier.
The flight was commanded by Captain Robert Albin "Bob" Loft, age 55, a veteran pilot ranked 50th in seniority at Eastern Air Lines. Captain Loft had been with the airline for 32 years and had accumulated a total of 29,700 flight hours throughout his flying career. He had logged 280 hours in the L-1011. His flight crew included First Officer Albert John "Bert" Stockstill, 39, who had 5,800 hours of flying experience (with 306 of them in the L-1011), and Flight Engineer Donald Louis "Don" Repo, 51, who had 15,700 hours of flying experience, with 53 of them in the L-1011.
A company employee—technical officer Angelo Donadeo, 47, returning to Miami from an assignment in New York—accompanied the flight crew for the journey, but was officially an off-duty, "nonrevenue passenger".
Flight 401 departed JFK Airport in New York on Friday, December 29, 1972, at 21:20EST, with 163 passengers and 13 crew members aboard.
The flight was routine until 23:32, when the airplane began its approach into Miami International Airport. After lowering the gear, First Officer Stockstill noticed that the landing gear indicator, a green light identifying that the nose gear is properly locked in the "down" position, had not illuminated. This was later discovered to be due to a burned-out light bulb. The landing gear could have been manually lowered, nonetheless. The pilots cycled the landing gear, but still failed to get the confirmation light.
Loft, who was working the radio during this leg of the flight, told the tower that they would discontinue their approach to their airport and requested to enter a holding pattern. The approach controller cleared the flight to climb to 2000feet, and then hold west over the Everglades.
The cockpit crew removed the light assembly, and Second Officer Repo was dispatched to the avionics bay beneath the flight deck to check via a small porthole whether the landing gear was indeed down. Fifty seconds after reaching their assigned altitude, Captain Loft instructed First Officer Stockstill to put the L-1011 on autopilot. For the next 80 seconds, the airplane maintained level flight. Then, it dropped 100feet, and then again flew level for two more minutes, after which it began a descent so gradual it could not be perceived by the crew. In the next 70 seconds, the airplane lost only 250feet, but this was enough to trigger the altitude warning C-chord chime located under the engineer's workstation. The engineer (Repo) had gone below, and no indication was heard of the pilots' voices recorded on the CVR that they heard the chime. In another 50 seconds, the plane was at half its assigned altitude.[5]
As Stockstill started another turn, onto 180°, he noticed the discrepancy. The following conversation was recovered from the flight voice recorder later:
Stockstill: We did something to the altitude.
Loft: What?
Stockstill: We're still at 2,000 feet, right?
Loft: Hey—what's happening here?
Less than 10 seconds after this exchange, the jetliner crashed. The location was west-northwest of Miami, 18.7miles from the end of runway 9L. The airplane was traveling at 227mph when it hit the ground. With the aircraft in mid-turn, the left wingtip hit the surface first, then the left engine and the left landing gear, making three trails through the sawgrass, each 5feet wide and more than 100feet long. When the main part of the fuselage hit the ground, it continued to move through the grass and water, breaking up as it went.
The TriStar's port outer wing structure struck the ground first, followed by the number1 engine and the port main undercarriage. The disintegration of the aircraft that followed scattered wreckage over an area 500m (1,600feet) long and 100m (300feet) wide in a southwesterly direction. Only small fragments of metal marked the wingtip's first contact, followed 15m (49feet) further on by three massive 35abbr=onNaNabbr=on swaths cut through the mud and sawgrass by the aircraft's extended undercarriage before two of the legs were sheared off. Then came scattered parts from the number 1 (port) engine, and fragments from the port wing itself and the port tailplane. About 150m (490feet) from the wingtip's initial contact with the ground, the massive fuselage had begun to break up, scattering components from the underfloor galley, the cargo compartments, and the cabin interior. At 250m (820feet) along the wreckage trail, the outer section of the starboard wing tore off, gouging a 18m (59feet) crater in the soft ground as it did so. From this point on, the breakup of the fuselage became more extensive, scattering metal fragments, cabin fittings, and passenger seats widely.
The three major sections of the fuselage—the most intact of which was the tail assembly—lay in the mud towards the end of the wreckage trail. The fact that the tail assembly—rear fuselage, number2 tail-mounted engine, and remains of the empennage—finally came to rest substantially further forward than other major sections, was probably the result of the number 2 engine continuing to deliver thrust during the actual breakup of the aircraft. No complete cross-section of the passenger cabin remained, and both the port wing and tailplane were demolished to fragments. Incongruously, not far from the roofless fuselage center section with the inner portion of the starboard wing still attached, lay a large, undamaged and fully inflated rubber dinghy, one of a number carried on the TriStar in the event of an emergency water landing. The breakup of the fuselage had freed it from its stowage and activated its inflation mechanism.
Robert "Bud" Marquis (1929–2008),[6] an airboat pilot, was out frog gigging with Ray Dickinsin (1929–1988) when they witnessed the crash. They rushed to rescue survivors. Marquis received burns to his face, arms, and legs—a result of spilled jet fuel from the crashed TriStar—but continued shuttling people in and out of the crash site that night and the next day. For his efforts, 35 years after the crash, he received the Humanitarian Award from the National Air Disaster Alliance/Foundation and the "Alumitech – Airboat Hero Award", from the American Airboat Search and Rescue Association.[7]
In all, 75 survived the crash—67 of the 163 passengers and eight of the 10 flight attendants. Despite their own injuries, the surviving flight attendants were credited with helping other survivors and several quick-thinking actions such as warning survivors of the danger of striking matches due to jet fuel in the swamp water and singing Christmas carols to keep up hope and draw the rescue teams' attention, as flashlights were not part of the standard equipment on commercial airliners at the time. Of the cockpit crew, only flight engineer Repo survived the initial crash, along with technical officer Donadeo, who was down in the nose electronics bay with Repo at the moment of impact. Stockstill was killed on impact, while Captain Loft died in the wreckage of the flight deck before he could be transported to a hospital. Repo was evacuated to a hospital, but later died from his injuries. Donadeo, the lone survivor of the four flight-deck occupants, recovered from his injuries. Frank Borman, a former NASA astronaut and Eastern's senior vice president of operations, was awakened at home by a telephone call reporting a probable crash. He immediately drove to Eastern's Miami offices and decided to charter a helicopter to the crash site, as the swampy terrain made rescue difficult, and Eastern Airlines had not heard any news of progress in rescue efforts. There he was able to land in a swampy patch of grass and coordinate rescue efforts. He accompanied three survivors on the helicopter to a hospital, including a flight attendant and a passenger who lost her baby in the crash.[8]
Most of the dead were passengers in the aircraft's midsection.[9] The swamp absorbed much of the energy of the crash, lessening the impact on the aircraft. The mud of the Everglades may have blocked wounds sustained by survivors, preventing them from bleeding to death. However, it also complicated the survivors' recuperation, as organisms in the swamp caused infection, with the potential for gas gangrene. Eight passengers became infected and were treated with hyperbaric chambers. All the survivors were injured; 60 received serious injuries and 17 suffered minor injuries that did not require hospitalization. The most common injuries were fractures of ribs, spines, pelvises, and lower extremities. Fourteen survivors had various degrees of burns.
The National Transportation Safety Board (NTSB) investigation discovered that the autopilot had been inadvertently switched from altitude hold to control wheel steering (CWS) mode in pitch. In this mode, once the pilot releases pressure on the yoke (control column or wheel), the autopilot maintains the pitch attitude of the aircraft until the yoke is again moved. Investigators believe the autopilot switched modes when the captain accidentally leaned against the yoke while turning to speak to the flight engineer, who was sitting behind and to the right of him. The slight forward pressure on the stick would have caused the aircraft to enter a slow descent, maintained by the CWS system.
Investigation into the aircraft's autopilot showed that the force required to switch to CWS mode was different between the A and B channels (15and, respectively). Thus, the switching to CWS in channel A possibly did not occur in channel B, thus depriving the first officer of any indication the mode had changed (channel A provides the captain's instruments with data, while channel B provides the first officer's).
After the aircraft had descended from the selected altitude of, a C-chord sounded from the rear speaker. This altitude alert, designed to warn the pilots of an inadvertent deviation from the selected altitude, went unnoticed by the crew. Investigators believe this was due to the crew being distracted by the nose gear light, and because the flight engineer was not in his seat when it sounded, so would not have been able to hear it. Visually, since it was nighttime and the aircraft was flying over the darkened terrain of the Everglades, no ground lights or other visual signs indicated the TriStar was slowly descending.
Captain Loft was found during the autopsy to have an undetected brain tumor in an area that controls vision. However, the NTSB concluded that the captain's tumor did not contribute to the accident.
The final NTSB report cited the cause of the crash as pilot error, specifically: "the failure of the flight crew to monitor the flight instruments during the final four minutes of flight, and to detect an unexpected descent soon enough to prevent impact with the ground. Preoccupation with a malfunction of the nose landing gear position indicating system distracted the crew's attention from the instruments and allowed the descent to go unnoticed."
In response to this and other accidents during the 1970s, many airlines started crew resource management training for their pilots.[10] [11] The training is designed to make problem solving in a cockpit much more efficient, thus causing less distraction for the crew. Flashlights are now standard equipment near jumpseats, and all jumpseats are outfitted with shoulder harnesses.[12]
During the following months and years, stories began circulating that employees of Eastern Air Lines and numerous passengers had reported sightings of dead crew members, Captain Robert Loft and Flight Engineer Donald Repo, sitting aboard other L-1011s (including, in particular, N318EA).[13] [14] [15] These stories speculated that parts of the crashed aircraft were salvaged after the investigation and refitted into other L-1011s.[13] [16] The reported hauntings were said to be seen only on the planes that used the spare parts.[13] [14] Gossip regarding the sighting of the spirits of Don Repo and Bob Loft spread throughout Eastern Air Lines to the extent that Eastern's management warned employees that they could be dismissed if caught spreading ghost stories.[14] While Eastern Air Lines publicly denied their planes were haunted, they reportedly removed all the salvaged parts from their L-1011 fleet.[15] Over time, the reporting of ghost sightings stopped. An original floor board from Flight 401 remains in the archives at History Miami in South Florida.[17] Pieces of Flight 401's wreckage can also be found in Ed and Lorraine Warren's Occult Museum in Monroe, Connecticut.[18]
The story of the crash and its aftermath were documented in John G. Fuller's 1976 book The Ghost of Flight 401.[19] Fuller recounts stories of paranormal events aboard other Eastern aircraft and the belief that these were caused by equipment salvaged from the wreckage of Flight 401.[20] A television movie adapted from Fuller's book, also titled The Ghost of Flight 401 and emphasizing the ghost sightings, was broadcast by NBC in February 1978.
Eastern Air Lines CEO (and former Apollo astronaut) Frank Borman termed the ghost stories about the crash "garbage."[21] Eastern considered suing for libel, based on assertions of a cover-up by Eastern executives, but Borman opted not to, feeling a lawsuit would merely provide more publicity for the book. Loft's widow and children did sue Fuller — for infringement of Loft's right of publicity, for invasion of privacy, and for intentional infliction of emotional distress — but the lawsuit was dismissed and the dismissal upheld by the Florida Fourth District Court of Appeal.[22]
According to Robert J. Serling's 1980 book From the Captain to the Colonel: An Informal History of Eastern Airlines, the claim that wreckage from Flight 401 was installed and later removed from other Eastern aircraft was false, and no Eastern employees had ever claimed to have seen or believed in the alleged ghost sightings. Skeptic Brian Dunning claims that the origin for the ghost sightings may have been a joke made by an Eastern Air Lines captain after an emergency landing in which he quipped that he "thought [Don] Repo's ghost was on the plane."[23]
The crash was documented in Rob and Sarah Elder's 1977 book Crash.[24] A television movie of the same name was broadcast in October 1978. Based on the book, it dramatized the crash, rescue efforts, and NTSB investigation. Eddie Albert featured as "Dunn", a fictionalized version of Captain Robert Loft.
Bob Welch's 1979 album Three Hearts includes a song titled "The Ghost of Flight 401."
Footage of the aftermath appears in the disaster documentary Days of Fury (1979),[25] directed by Fred Warshofsky.
The accident and the subsequent ghost story were mentioned by Dan Aykroyd during his appearance on The Tonight Show Starring Johnny Carson on June 6, 1984.
Flight 401 is mentioned in Supernatural S1E4 "Phantom Traveler" (2005).[26]
The crash was featured in the Discovery Channel Canada/National Geographic TV series Mayday, in S5E44 "Fatal Distraction" (2008).[27]
It is featured in Why Planes Crash S1E3 "Human Error" (2010).
A similar situation appeared in the Thai movie Dark Flight (2012), directed by Kongkiat Khomsiri.
The Ghosts of Flight 401, part of the Discovery+ series Shock Docs, emphasizes the supernatural legacy of the crash.[28]